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Originally Posted by OldAg84
I think this was an MD test flight gone awry. I think I read somewhere the reattached the piece and the plane flew again. Does anyone know the real story behind the video and where the plane may have wound up?
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My friend Jay, owner of the Alexis Park Inn (best crash/weird incident page on the Net BTW) says: "This was an early DC-9/MD-80 certification test. After this little demonstration they beefed up the tail section -- for obvious reasons!"
And the NTSB had this to say about the matter:
http://www.alexisparkinn.com/Photoga...t/AAR82-02.pdf
During a landing distance certification at Edwards AFB in May 1980, the ATP engineering test pilot was using a HUD doing some exotic pitch v. descent stabilization concept using only power to control sink rate (??? Ok for stabilizing approach but - no flare?). Keeping the pitch attitude fixed & stable
all the way to touchdown 
(???) for some reason I don't understand. Basically he intentionally didn't flare much if at all, only tried to flare 1 second before touchdown - I mean impact- and never broke the sink rate. Until the sink rate broke his nice airplane.