For any former P-3 guys out there, incident occured earlier this week, here's the info I received:
Aircraft departed Whidbey Island (BUNO 161331) for a FCF flight. They were at 160 KIAS, approach flaps during a prop fails to feather check on #1 when #2 started surging. They bagged #2, but while doing so got to 122 KIAS. When they added power, they were way below VMC, and departed controlled flight. About a minute later, just before impact, they recovered.
45 consecutive rivets were pulled out on the starboard wing during the 7G pull out (rolling pull), after peaking at negative 2.4g's as well. It’s reported they did five spin rotations from 5500 ft - they bottomed out "between 50 and 200 ft"!! The inside of the fuel tanks were visible from pulled panels when they landed. This being categorized as a Class-A mishap.