Originally Posted by
PNWFlyer
it failed on 3 previous flights. All those crews handled the emergency just fine.
on the last second flight yes. It was replaced with a counterfeit part and pencil whipped. Failed when crew took off. They disable the stick shaker and flew from Bali to Jakarta with the stab cutout switched off. Then only wrote up the unreliable airspeed, not the AOA issue. Plane crashed the next morning.
they also forgot to mention the Ethiopian crew turn the stab trim switches back on to try and engage the autopilot.
they also forgot to mention the FAA retained certification for MCAS. They did now about the expanded envelope and that was in the DOJ report.
They got the merger stuff right but we’re wrong about the anything about the MAX. MCAS was about certification flights. Stick force per G. It was not to push the nose down like the media loves to say.
I’m not doubting you, but where did you find that information?
I’d like to have it when I talk the folks who only watch cable news.