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Old 03-02-2008, 03:52 PM
  #31  
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Downside is sounds like they weren't losing ALL braking, just braking to the left mains....or at least part of the mains.
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Old 03-02-2008, 07:11 PM
  #32  
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Originally Posted by own nav View Post
From my best sources in Jackson, the plane touched down with only a couple thousand feet of runway left. Sounds like they were going too fast on the approach. I'm surprised this hasn't recieved more attention.
In addition to posting this most recent newspaper story, it would seem to me that an apology is due from 'own nav.' A good lesson learned about some of those so-called "sources" that come out of the woodwork after an accident or incident . . .
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Old 03-03-2008, 06:27 AM
  #33  
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Originally Posted by cactusdog16 View Post
In addition to posting this most recent newspaper story, it would seem to me that an apology is due from 'own nav.' A good lesson learned about some of those so-called "sources" that come out of the woodwork after an accident or incident . . .
I already apologized for the speculation before the report came out. Look back a page or 2.

This is one big piece of the puzzle, Lambourne was right about it, we haven't recieved the full story yet.
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Old 03-03-2008, 10:16 AM
  #34  
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More from the NTSB:

http://www.denverpost.com/breakingnews/ci_8410891

Crossed wires may have caused United jet skid
By Jeffrey Leib
The Denver Post

Article Last Updated: 02/29/2008 05:34:39 PM MST



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Air safety investigators said today that a United Airlines jet may have skidded off a runway after landing Monday evening at the Jackson Hole Airport because braking system wires were cross-connected.
The National Transportation Safety Board said after its investigators examined the left main landing gear brakes, they determined that the inboard and outboard wheel speed tachometer wires were crossed, a condition that would affect braking capability and the antiskid system.
The Airbus A320 jet, which had flown from Denver International Airport to the Wyoming city as Flight 267, ended up 116 feet past the end of the runway and 140 feet to the right of the runway centerline, NTSB said. The incident occurred about 9:16 p.m.
The plane's two pilots, four flight attendants and 119 passengers evacuated the plane via emergency slides and no serious injuries occurred, according to the safety board.
NTSB said it also is investigating why one of the emergency slides did not inflate after it deployed.
The agency said it is looking at an event from last October with "similar circumstances" to the Jackson Hole incident when another Airbus A320 operated by United "exited" a runway and hit runway lights after landing at Chicago's O'Hare International Airport.
In Monday's incident, investigators found a heavy skid mark on the runway associated with the inboard tire of the left main landing gear, NTSB said. "This tire was found deflated and showed wear consistent with a skid."
Crossing of the tachometer wires would likely "cause the antiskid system to use the inboard wheel speed to control outboard braking, and vice versa," NTSB said in its preliminary report.
"In such a situation, it would be likely that when the inboard tire began to skid, the antiskid system would release the pressure on the outboard brake instead of the inboard brake." NTSB said an examination of the plane's maintenance records showed that both main landing gear units on the A320 were replaced in early February.
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