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Originally Posted by magiccarpet
(Post 3747770)
Hearing some noise now that the crew may have been trying to control the pressure manually. Seems like this plane was having issues with its auto controllers. Is it possible that they inadvertently closed the valve completely, overwhelming the two pressure relief valves causing the door to blow out like it did? Seems like these plug doors would be the next weakest thing to give way.
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Originally Posted by Jetlikespeed
(Post 3747837)
Buddy work at horizon for 100 hours before getting hired at frontier and is an expert on 121 AQP programs 🤡
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Originally Posted by FAR121
(Post 3747934)
i highly doubt AK MX would be to blame. They would state the case that even if they needed to put the pressurisation Auto system on MEL that the plug could have fallen off even on AUTO mode. Would have taken enough cycles. Not armchair QBing how the crew handled the manual pressurising system but who knows.
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Originally Posted by FAR121
(Post 3747934)
i highly doubt AK MX would be to blame. They would state the case that even if they needed to put the pressurisation Auto system on MEL that the plug could have fallen off even on AUTO mode. Would have taken enough cycles. Not armchair QBing how the crew handled the manual pressurising system but who knows.
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Originally Posted by av8or
(Post 3747942)
Article also said that the decompression was strong enough to “blow the cockpit door open”…. which seems odd for a number of reasons. Can anyone confirm that happening?
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Originally Posted by Smooth at FL450
(Post 3748064)
If the airplane was over pressurizing, people would have noticed. There were no blown ear drums. The PSI delta was probably around 2-4. Journalism paranoia. |
Originally Posted by FAR121
(Post 3747839)
The cockpit voice recorder data on the Alaska Airlines Boeing 737 MAX 9 jet which lost a panel mid-flight on Friday was overwritten, U.S. authorities said, renewing attention on an industry call for longer in-flight recordings.
National Transportation Safety Board (NTSB) chair Jennifer Homendy said on Sunday no data was available on the cockpit voice recorder because it was not retrieved within two hours - when recording restarts, erasing previous data. Did someone forget that part of the NTSB checklist or was the flight from and back to PDX so long that the CVR ended up hitting the 2 hour mark and overwriting itself? |
Found the plug: https://pbs.twimg.com/media/GDWAFwJa...name=4096x4096
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Originally Posted by av8or
(Post 3747948)
Article on Reuters says they found the door… so that’s good. Article also said that the decompression was strong enough to “blow the cockpit door open”…. which seems odd for a number of reasons. Can anyone confirm that happening?
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