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-   -   Max 9s to be Grounded (https://www.airlinepilotforums.com/united/145814-max-9s-grounded.html)

Merequetengue 01-08-2024 09:26 AM

https://x.com/airlineflyer/status/17...tOrnMdFOUu0MqA

Hopefully it will not take so long

MasterOfPuppets 01-08-2024 11:46 AM


Originally Posted by Merequetengue (Post 3748021)

i have heard that United already did what they assumed would be the AD and we’re standing by to see what additional items needs to be inspected.

I think the majority of our aircraft just need to have there side walls snapped back on and seats reinstalled and they will be good to go. Tomorrow might look fairly normal.

DWC CAP10 USAF 01-08-2024 01:21 PM


Originally Posted by JohnnyBekkestad (Post 3746947)
as long as they don’t find bunch of airplanes with similar problems.

https://theaircurrent.com/feed/dispa...9-inspections/

iahflyr 01-09-2024 06:32 AM

Does anyone know how many Max 9’s have been returned to service?

Chuck D 01-09-2024 06:44 AM

Have any at all? Do they know whether this is isolated to those specific plugs or whether it's a broad QC process that failed to catch that and was responsible for far more?

Dave Fitzgerald 01-09-2024 09:09 AM


Originally Posted by Chuck D (Post 3748450)
Have any at all? Do they know whether this is isolated to those specific plugs or whether it's a broad QC process that failed to catch that and was responsible for far more?

It's starting to look like the 2 bolts that are installed to keep the latch from moving were missing. Looks like the design is fine, but you have to install the bolts....

It'll be an inspection process to see if the bolts are there and properly torqued. Hopefully, the process has been fixed at Boeing, and they won't find any more problems. I'm surprised, if the bolts were not installed, it lasted 145 flights.

JackReacher 01-09-2024 11:30 AM


Originally Posted by Dave Fitzgerald (Post 3748547)
It's starting to look like the 2 bolts that are installed to keep the latch from moving were missing. Looks like the design is fine, but you have to install the bolts....

It'll be an inspection process to see if the bolts are there and properly torqued. Hopefully, the process has been fixed at Boeing, and they won't find any more problems. I'm surprised, if the bolts were not installed, it lasted 145 flights.

Boeing really needs to get their act together. This type of quality control issue at this level is unconscionable. Absolutely no excuse.

hamsandwich 01-09-2024 12:05 PM


Originally Posted by JackReacher (Post 3748614)
Boeing really needs to get their act together. This type of quality control issue at this level is unconscionable. Absolutely no excuse.

They wont learn anything from this. Nothing will change. Boeing will continue to suck until the end of time.

list 01-09-2024 12:36 PM

Agree, this level of constant neglect has no place in the airplane making business. Too much money wrapped up in carriers needing delivered planes flying and to be delivered planes delivered. So lucky no one was killed. Whelp, until the next 'discovery'

nene 01-09-2024 01:03 PM


Originally Posted by Dave Fitzgerald (Post 3748547)
It's starting to look like the 2 bolts that are installed to keep the latch from moving were missing. Looks like the design is fine, but you have to install the bolts....

It'll be an inspection process to see if the bolts are there and properly torqued. Hopefully, the process has been fixed at Boeing, and they won't find any more problems. I'm surprised, if the bolts were not installed, it lasted 145 flights.

Apparently putting a MAX together is like putting the shelves together from IKEA and afterwards having about 8 bolts left over.


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