737 MAX grounded
#511
Gets Weekends Off
Joined: Nov 2009
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Weren’t they already traveling at ludicrous speed at that point? Those trim wheels take a little muscle at normal air loads, I imagine that they are difficult when you’re beyond that point. Also, they turned the switches off, stopped the trim command, and then decided to turn them back on so that they could use electric trim to get the nose up. Both crashes were a combination of equal parts bad design and bad piloting.
It’s a **** poor design of a transport category airplane that at this juncture, is too big to fail.
#512
Gets Weekends Off
Joined: Jan 2012
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Having flown 737 NG with manual stab trim after stab out of trim light on at 15,000’ I can say this.
At 250 kias forward manual trim was easy and smooth operating. Nose up trim was difficult and was not smooth.
It would have been extremely difficult/impossible to get ANY manual nose up trim at the 400 plus kias that they were at.
I would like a no look scenario in the sim.
Something no one has mentioned. MCAS is only active after flaps up. I would consider extending flaps to 1 if cut out switches proved to be ineffective. That being said, is it a function of flap position or flap handle position??
At 250 kias forward manual trim was easy and smooth operating. Nose up trim was difficult and was not smooth.
It would have been extremely difficult/impossible to get ANY manual nose up trim at the 400 plus kias that they were at.
I would like a no look scenario in the sim.
Something no one has mentioned. MCAS is only active after flaps up. I would consider extending flaps to 1 if cut out switches proved to be ineffective. That being said, is it a function of flap position or flap handle position??
#513
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Joined: Apr 2016
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#514
Weren’t they already traveling at ludicrous speed at that point? Those trim wheels take a little muscle at normal air loads, I imagine that they are difficult when you’re beyond that point. Also, they turned the switches off, stopped the trim command, and then decided to turn them back on so that they could use electric trim to get the nose up. Both crashes were a combination of equal parts bad design and bad piloting.
#515
The FAA should mandate that every MAX pilot flies the exact profiles (in
a MAX sim) that downed those two planes. Cold turkey, no advance warning, just lifting off as a 'first look' maneuver. With the software exactly as they flew the jet.
Only after everyone passes with flying colors will I agree with those who claim that simply flipping the Stab Cut Out switches was the solution.
a MAX sim) that downed those two planes. Cold turkey, no advance warning, just lifting off as a 'first look' maneuver. With the software exactly as they flew the jet.
Only after everyone passes with flying colors will I agree with those who claim that simply flipping the Stab Cut Out switches was the solution.
#516
I think that a number of people at Boeing should be investigated for actions that violate our criminal justice code.
The whole board, and all of upper management should have already resigned...
https://www.theatlantic.com/ideas/ar...arings/602188/
https://theoutline.com/post/8269/the...=1&zi=h47uyaim
https://www.ccn.com/10-blunders-that...7-max-forever/
The whole board, and all of upper management should have already resigned...
https://www.theatlantic.com/ideas/ar...arings/602188/
https://theoutline.com/post/8269/the...=1&zi=h47uyaim
https://www.ccn.com/10-blunders-that...7-max-forever/
#517
I was hoping that Boeing would have stopped at the max 9 after the crisis and either built a new airplane or revamp the 757.
I just saw the other day they are rolling out the dash 10 abomination.
They have learned nothing from this debacle except to continue profits over safety and common sense. New management is needed desperately!
Boeing use to build magnificent airplanes but haven’t since the 777.
Although the 787 is good now it had a rough start and because of outsourcing and profits over safety they were lucky they didn’t have a hull loss.
I just saw the other day they are rolling out the dash 10 abomination.
They have learned nothing from this debacle except to continue profits over safety and common sense. New management is needed desperately!
Boeing use to build magnificent airplanes but haven’t since the 777.
Although the 787 is good now it had a rough start and because of outsourcing and profits over safety they were lucky they didn’t have a hull loss.
#518
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Joined: Jul 2008
Posts: 874
Likes: 1
They did not cut out the stab trim until the trim position was nearly full nose-down and was flying at over Vmo (over 390kts vs Vmo of 340kts). When they turned the stab trim back on the captain repeatedly tried to engage the autopilot (which won't engage when out-of-trim) instead of using the primary electric trim, which might have had a chance of rolling the trim back up. That allowed additional unscheduled MCAS activations to roll it to the full nose-down stop.
The Captain didn't know what to do so he kept trying to engage the autopilot. He had tried the same thing less than 500' off the ground on takeoff (minimum autopilot engagement altitude on takeoff is 800'). In doing so, he briefly coupled the autopilot (CMD A) to the Flight Control Computer that was receiving bad data. This produced unstable pitch inputs from the autopilot and caused the autopilot to disconnect within 30 seconds.
While "STAB TRIM CUTOUT switches ... CUTOUT" is part of the applicable procedure, they did it far too late and without doing the previous steps--this one is the second-to-last step. Doing only one item on a checklist does not qualify as following the procedure.
They made many other procedural errors prior to that one including never just flying the airplane. i.e. when the nose gets heavy, trimming it back up with the primary electric trim. The Captain of the Lion Air accident flight kept the airplane in-trim through 21 unscheduled MCAS activations by doing just that. The trim didn't get significantly out-of-trim until he transferred control to the F/O who did not re-trim the airplane after each MCAS activation.
If you're interested in understanding the actions of both accidents crews, I'd recommend this (rather long) article from NY Times Magazine. It is the most detailed article that I have seen on the MAX crashes.
https://www.nytimes.com/2019/09/18/m...x-crashes.html
The Captain didn't know what to do so he kept trying to engage the autopilot. He had tried the same thing less than 500' off the ground on takeoff (minimum autopilot engagement altitude on takeoff is 800'). In doing so, he briefly coupled the autopilot (CMD A) to the Flight Control Computer that was receiving bad data. This produced unstable pitch inputs from the autopilot and caused the autopilot to disconnect within 30 seconds.
While "STAB TRIM CUTOUT switches ... CUTOUT" is part of the applicable procedure, they did it far too late and without doing the previous steps--this one is the second-to-last step. Doing only one item on a checklist does not qualify as following the procedure.
They made many other procedural errors prior to that one including never just flying the airplane. i.e. when the nose gets heavy, trimming it back up with the primary electric trim. The Captain of the Lion Air accident flight kept the airplane in-trim through 21 unscheduled MCAS activations by doing just that. The trim didn't get significantly out-of-trim until he transferred control to the F/O who did not re-trim the airplane after each MCAS activation.
If you're interested in understanding the actions of both accidents crews, I'd recommend this (rather long) article from NY Times Magazine. It is the most detailed article that I have seen on the MAX crashes.
https://www.nytimes.com/2019/09/18/m...x-crashes.html
#519
Banned
Joined: Mar 2018
Posts: 1,358
Likes: 0
They did not cut out the stab trim until the trim position was nearly full nose-down and was flying at over Vmo (over 390kts vs Vmo of 340kts). When they turned the stab trim back on the captain repeatedly tried to engage the autopilot (which won't engage when out-of-trim) instead of using the primary electric trim, which might have had a chance of rolling the trim back up. That allowed additional unscheduled MCAS activations to roll it to the full nose-down stop.
The Captain didn't know what to do so he kept trying to engage the autopilot. He had tried the same thing less than 500' off the ground on takeoff (minimum autopilot engagement altitude on takeoff is 800'). In doing so, he briefly coupled the autopilot (CMD A) to the Flight Control Computer that was receiving bad data. This produced unstable pitch inputs from the autopilot and caused the autopilot to disconnect within 30 seconds.
While "STAB TRIM CUTOUT switches ... CUTOUT" is part of the applicable procedure, they did it far too late and without doing the previous steps--this one is the second-to-last step. Doing only one item on a checklist does not qualify as following the procedure.
They made many other procedural errors prior to that one including never just flying the airplane. i.e. when the nose gets heavy, trimming it back up with the primary electric trim. The Captain of the Lion Air accident flight kept the airplane in-trim through 21 unscheduled MCAS activations by doing just that. The trim didn't get significantly out-of-trim until he transferred control to the F/O who did not re-trim the airplane after each MCAS activation.
If you're interested in understanding the actions of both accidents crews, I'd recommend this (rather long) article from NY Times Magazine. It is the most detailed article that I have seen on the MAX crashes.
https://www.nytimes.com/2019/09/18/m...x-crashes.html
The Captain didn't know what to do so he kept trying to engage the autopilot. He had tried the same thing less than 500' off the ground on takeoff (minimum autopilot engagement altitude on takeoff is 800'). In doing so, he briefly coupled the autopilot (CMD A) to the Flight Control Computer that was receiving bad data. This produced unstable pitch inputs from the autopilot and caused the autopilot to disconnect within 30 seconds.
While "STAB TRIM CUTOUT switches ... CUTOUT" is part of the applicable procedure, they did it far too late and without doing the previous steps--this one is the second-to-last step. Doing only one item on a checklist does not qualify as following the procedure.
They made many other procedural errors prior to that one including never just flying the airplane. i.e. when the nose gets heavy, trimming it back up with the primary electric trim. The Captain of the Lion Air accident flight kept the airplane in-trim through 21 unscheduled MCAS activations by doing just that. The trim didn't get significantly out-of-trim until he transferred control to the F/O who did not re-trim the airplane after each MCAS activation.
If you're interested in understanding the actions of both accidents crews, I'd recommend this (rather long) article from NY Times Magazine. It is the most detailed article that I have seen on the MAX crashes.
https://www.nytimes.com/2019/09/18/m...x-crashes.html
#520
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Joined: Apr 2016
Posts: 381
Likes: 0
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